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05-10-1999 Council Packet
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05-10-1999 Council Packet
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site designer has been in contact with the City's On-Site Septic Systems Manager, Steve Weckman. <br />Staff will attach a septic report as an Exhibit to this report when it is available. <br />ACCESS <br />The preliminary plat has been reviewed by the City Engineer. The proposed location for the private <br />road appears acceptable. It has been sent to Hennepin County for review. The proposed street <br />section will need to be 28* to meet city standards because the number of units to be served exceeds <br />7. Water from the private road shall ^ diverted from Old Crystal Bay Road (County Road 84). <br />GRADING <br />There is an existing ditch on this parcel which serves as a drainage way for a pond. A driveway for <br />proposed Lot 3 may cross this ditch. If so, it should not impede flows through the existing ditch. The <br />final plan needs to identify all structures to be removed. A grading and erosion control plan should <br />be submitted for the entire site for review. Erosion controls should be in place before any grading <br />to protect the wetland. Erosion control measures will be required during construction of the houses <br />emd septic sites. <br />DRAINAGE <br />The site is located within the French Lake Drainage district. The site drains southerly to an existing <br />wetland along the south edge of the site. Storm water drains to the wetland from the north to the <br />south. The flow from the north is routed through an existing ditch. Ditch stabilization may be <br />required if the flow will continue to route through it. An alternative would be to install storm sewer <br />to convey flows from north of the site to the stormwater management pond. The pond would need <br />to be sized if this is the proposed drainage method. There is a 36" pipe for a southerly outlet of the <br />existing wetland. The city's proposed stormwater management plan states that water quantity may <br />be a problem downstream and recommends restricting the size of the pipe to 27". Reducing the <br />outlet pipe would result in a reduction of the rate of stormwater downstream but would increase the <br />high water level of the wetland to 966. The City Engineer will need to review the wetland outlet <br />sizing after a drainage area map, storm sewer, and ponding calculations are provided. The <br />calculations should be based on the total drainage area that flows into the wetland. The plans will <br />need to be submitted to the Minnehaha Creek Watershed District (MCWD). <br />EASEMENTS <br />The City Engineer has recommended that a 10 ’ trail easement be dedicated along the west property <br />line adjacent to Old Crystal Bay Road. Internal and perimeter drainage and utility easements shall <br />be provided 5' along all interior lot lines and 10' along perimeter lines. Drainage easements shall be <br />#2477 Stickney <br />250 & 340 Old Crystal Day Road South <br />Subdivision <br />PC-4/19/99 <br />page~6
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