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HomeMy WebLinkAbout1978-02-13 Septic System Design Report' An Expansion of Soil Engines ing Services, Inc.0mun- ENONEERM TESTMrO 'O MINNEAVOLIS/ST. VAUL 6680 S. County Rd. 18, V.O. Box 36108, Myb., Mn. 56435 / 612.941-SM 1 a axAU%F. E.. AseuAnr ❑ NORTHERN MINNESOTA 3219 E. 19tb Awnw, Hibbing, MN. 56746 / 219.2634M 1,N ANOEnEOa, VbAm Operations O CENTRAL MINNESOTA 200 Owo Awnw No., St. Cloud, Mo. 5=1 if612.253.9940 C O. KxUU P. E., V"Flat Ee A@W.V February 13, 1978 Mr. David Nitz 464 2nd Street Excelsior, MN SS331 Re: 78-08B SOIL BORINGS & PERCOLATION TESTS Lot 8, Block 1 Brown's Residence Farview Addition Orono, Minnesota Gentlemen: As you requested, we have recently c-zducted a series of two power auger borings and 21 percolat i tests in an attempt to evaluate soil absorptivity rates tor an individual sanitary system proposed for the above referenced lot. The boring and percolation tests were taken at the locations as shown on the attached sketch. Field locations were determined by our crew with reference to the staked property corners. Surface elevations were referenced to a top -of - block marker set in a tree on the property line approxi- mately 20 feet north of the southeast property corner. An elevation of 100.0 was assumed for this bench mark. Initially, six percolation tests were conducted on the lot ' on January 6, 1978. At that time, all of the testL indi- cated failing results. As you requested then, six addi- tional were conducted slightly upgrade and farther to the north of the initial tests. Three of these tests numbered P-2, P-10 and P-12, all were within the minimum requirement for a drainfield. The three tests conducted further to the east in this series, however, all failed to meet the criteria for an adequate drainfield system. Subsequently, three additional tests were then conducted to the west of the ' three passing tests; however, these three also failed to meet the 60 mpi requirement. Six additional percolation tests and an additional soil boring were then conducted on ' February 9 in the area of the northeast portion of the lot, results also indicating this area to be unsuitable for a drainfield. 1 CONSULTING ENGINEERS/SOILS AND MATERIALS Test Borings - Foundation Engineering and Recommendations - Inspection of Cc ruction - Material Tasting of Soils. Concrots and Building "omponents 78-08B Mr. David Nitz -2- February 13, 1978 The percolation tests and the borings were either conducted with a truck -mounted power auger unit; or, in those areas inaccessible to truck, with a hand operated drill. All operations were c..►ducted in conformance with City of Orono specifications and in accordance with those procedures as indicated to you in previous percolation test reports conducted for various lots in the addition. The borings were probed immediately after their completion to check for the presence of groundwater and once again the following day. Groundwater was encountered at the 4-foot depth in boring B-1, however, was not enc untered at the time of the final reading in boring B-2. RESULTS: The log of soils encountered in the borings and the water level observations are shown on the att:+.h,2d Log of Boring sheets. Soil boring B-1 generally encountered a frozen silty clay topsoil to a depth of approximately '.�j feet, underlain by a silty clay lacustrine deposit to a depth of 8 feet. Silty clayey sand glacial till was then encountered to the 17-foot termination depth in this boring. Boring B-2 encountered a silty sandy clay topsoil from the surface to approximately the 1h-foot depth. A sandy clay glacial till was then encountered immediately below this layer to the 8-foot depth where a silty clayey sand till was then encountered to the 20-foot termination depth in the boring. The results of the percolation tests indicating the soil absorptivities in minutes per inch (mpi) are as follows: Surface Soil At Test N Elevation Test Depth P-1 92.5 Silty Clay (CL) P-2 93.5 Silty Sand (SM) P-3 92.3 Silty Clay (CL) P-4 91.3 Silty Clay (CL) P-5 92.2 Silty Clay (CL) P-6 92.5 Silty Clay (CL) P-7 91.8 Silty Clay (CL) P-8 98.4 Silty Clayey Sand, (SM- SC) P-9 92.6 Silty Clay (CL) P-10 96.9 Silty Clayey Sand, (SM-SC) Rate m i 80 30 120 240 80 75 40 BRAUR" ENGINEERING TESTING 78-08B Mr. David Nitz Test N P-11 P-12 P-13 P-14 P-15 P-16 P-17 P-18 P-19 P-20 P-21 Surface Elevation 9i. 2 94.8 94.1 93.5 94. 7 10S. 8 10S.4 106.7 107.6 105.9 107.2 -3- Soil At Test Depth February 13, 1978 Rate Lmp ij- Silty Clay (CL) Silty Clayey Sand, (SM-SC) Silty Clayey Sand, (SM-SC) Silty Cl.,y (CL) Silty Clayey Sand, (SM-SC) Sandy Clay (CL) Sandy Clay (CL) Sandy Clay (CL) Sandy Clay (CL) Sandy Clay (CL) Sandy Clay (CL) *No drop in water level observed. 60 120 240 120 * 480 * * * 480 As shown above, only three of the 21 percolation tests conducted on the lot met the specified minimum standard required for a drainfield system. As noted, some of the areas indicated passing results while no water movement was observed in other areas. This variability in the test results can probably be attributed to one or two factors. Soils in the test holes, particularly in the lower areas, appear to range from silty clays to silty clayey sand which would influence the percolation rate. The more cohesive sandy clays and silty clays would typically have higher percolation readings. The failing rates may also be affected by frost action. Although frost depth throughout the site appears to be somewhere between 1 and 2 feet below the surface, temperature measurements on another lot in Orono conducted February'll indicated that the soil temperature at the 36-inch depth was 320 F. If the water does not freeze when entering the soil, it would be considerably more viscuous, which would limit its flow through the soil pores. PRELIMINARY RECOMMENDATIONS: In a recent telephone conversation with Mr. Mike Gaffron, Septic System Inspector from the City of Orono, we have indicated that a potential drainfield system can likely be established on the lot in the area immediately to the west of the house, based on percolation tests NP-2, P-8, P-10, and P-12. The City has asked that we make a preliminary BRAUR'" ENGINEERING TESTING 78-08B Mr. David Nitz -4- February 13, 1978 design for a system in this area, subject to change, based on percolation tests run next spring. However, it would be based on a rate of on the orda rof 80 mpi, which is above the normal minimum acceptable standards. Although standards have not been set up for developing a system based on an 80 mpi rate, a larger than normal system consisting of seven 30-inch wide trenches, 75 feet in length, with 7 foot center -to -center spacing may be adequate for this system. This rate was interpolated from the standard curve system which indicates requirement rates per bedroom based on the minutes per inch reading. Based on this system, a typical 4-bedroom home would then require approximately 325 lineal feet of absorptive trench per bedroom. Although a system of this stature appears feasible, there is some risk of future failure. A sewage treatment mound would be the second alternative for the site. With this system, sand and rock fill can be placed directly on the natural clayey soils in the proposed drainfield area. It should be noted that general topography in this area should be relatively flat, with less than 3t grade slope. This system would be developed based on 125 square feet per bedroom or .83 square feet per gallon of waste per day. For a proposed 4-bedroom home, the mound'bed would require 500 square feet of total area. This can be accomplished with a bed length of 50 feet and a maximum width of 10 feet. The system then consists of approximately 12 inches of sand fill overlying the natural soils. A 9- inch layer of 3/4 to 2�-inch clean rock is then placed directly over the sand and used as a bedding for the pipe. A sandy soil should then be placed over the pipe, the thick- ness of which should be between 6 and 12 inches. A 6-inch layer of topsoil would then be placed immediately over the sand. The sideslopes of the dike should not be steeper than 3 feet horizontally to 1 foot vertically. If either of the two above systems are not feasible for the lot, a third alternative would be a sewage osmosis system. The sewage osmosis system can be useful in areas of heavy clay soils and in areas where the seasonal water table is high. This patented system, using a set of cathodes and anodes, together with the special drainfield trenches, should be designed, constructed, and maintained by a licensed dealer. This system, as well as those mentioned above, are, of course, all subject to City of Orono approval. s�un EN(i1NEERINQ TESTING 1 78-OSB Mr. David Nitz -S- February 13, 1978 ' It is recommended that additional percolation tests be conducted after the spring thaw in the event that frost action is, in fact, contributing to the failing results. ' If this proves to be the case, a more suitable drainfield system could then be developed on the lot. ' Should you have any further questions regarding these data or if we may provide further services on this project, kindly contact us at your convenience. Very truly yours, ;UN ENGINEERING TESTING, INC. Dennis M. Rietschel io �En. gineeI�rr'ng gist PVice President - Engineerilig DMR/CGK:skh ' The content of this report end supporting documents are for the exclusive use of the addressee In the absence of our prior written approval we make no representation and assume no responsibility to any other parties regarding such content BRAUR ENOWERING TE8T1N0 tiN�4�tl�it iNT�L F1EY. ! ol40 BRAUR" ENGINEERING TESTING --t�WZ9 4V"R 4WlAA- -� coc4nmj MrdU4 / t9c, 7— ^- ARV/fW 4owil2av WA MINW, /?- LOG OF BORINGS PROJECT: 78-008 Soil Borings S Percolation Tests DATE: 1/6/78 Lots 3 and 10, Block 1, Farview Addition SCALE: V-4' Orono, Minnesota BORING: B-1 LOCATION: Lot 8, BORING: B-2 LOCATION: R Block 1, See Attached See Attached Sketch. R 92.2 Sketch. 107.1 Depth AS De scr 148 ion o Materials ASTM D2 87 WL DepthDescr ono Al MaterialsD2487 ASTM W SILTY CLAY, black, CL SILTY SANDY AY, black, 1.5 frozen. (Topsoil) 1.5 frozen. (To P (Topsoil) CL SILTY CLAY, dark brown, SANDY CLAY, with a trace wet. of fine to medium CL (Lacustrine) CL Gravel, brown, moist. (Glacial Till) 8 8 SILTY CLAYEY SAND, fine SILTY CLAYEY SAND, fine to medium -grained, SM-SC to medium -grained, with SM-SC grayish brown, water- a trace of fine to med1wi bearing. Gravel, brown, moist to (Glacial Till) wet. (Glacial Till) 17 Water level down 8' 10 minutes after completion of boring. 20 Water level down 4' 24 Water level not encountered hours after completion of 10 minutes after completion of boring. boring. Bench Mark - Top of block Water level not encountered 24 marker in tree located 20'N hours after completion of of N.E. property corner with boring. elevation assumed - 100.0'. DESCRIPTIVE TERMINOLOGY PARTICLE SIZE IDENTIFICATION "AdtMs over 3" Cke Come 1 " — 3" Medium 1/4, — 1" Fine No. 4 — 1/2" Send Coro No. 4 —No. 10 Madum No. 10 — No. 40 Fine No. 40 — No. 100 Very Fine No. 100 — No. 200 Salt No. 200 — A01 mm Clay leN then A01 mm h _ , ATI VE DENSITY OF COHESIONLESS SOILS WV lopes 0 — 4 8PF boo S — 10 MF madam dense 11 — 30 9PF dew 31 — 60 S►F very dense SO► MF RELATIVE PROPORTIONS SOIL INTRUSIONS THICKNESS stern 1 IS" — 1 " Inver I" — 12" vervad alternating teeny Of lenses of clays and silts in lake deposit MOISTURE CONTENT Dry law than S% Moist sandal optimum moisture Net ovar optinwm noisture Wl.nrbsering saturated send CONSISTENCY OF COHESIVE SOI LS very soft 0 — 1 S►F soft 2 — 3 SPF rather colt 4— S BPF medium 6— 6 SFF rather stiff S — 12 BPF stiff 13 — 16 BFF very stiff 17 — 30 5PF hard 30+ S►F RELATIVE ►RO►OMYOINE with a few 0 — 10% with sorrel 11 — 20% with over 20% ORGANIC CONTENT 0 - S% non to slightly organic 6 — 10% slightly organic 11 — 26% organic 26 — 66% muck 66+ peat PLASTICITY OF SOILS WITH LESS THAN 20% CLAY eon plastic gritty, cannot thread slightly plastic rough to smooth, hard to thread plastic smooth to wary. easy to thread OF GRAVEL LABORATORY TESTS a trots 0 — S% DO Dry Density, pef OC Organic Content. % a little 6 — 1S% WD Net Density, gad S Percant of Saturation, % some 16 — 30% MC Natwal Moisture Content, % SG Specific Gravity and 31 — SO% LL Liquid Limit, % C Cohesion PL Plastic Limit, % 0 Angle of Internal Friction ►l Plasticity Index, % qu Unconfined Compressive Strength DRILLING NOTES: Standard penetration Not borings were advanced by 216" or 3%" I.D. hollow -stem augers unless noted other- wise. Jetting water was toed to clean out sugar prior to sampling only when indicated on log. Standard Penetration test brings we designated by the prefix -sr, (Split Tuba). Power auger brie* owe advanood by 4" or 6" diameter, continuous flits, solid stem augers. Soil classification and ovate depth are inferred from disturbed Nmplas supred to the surface and we therefore somewhat approximeta. ►over sugar brings we designated by the prefix "B' Hand probings ware advanced manually voth a 116" diameter probe and an limited to the depth from which the probe can be manually withdrawn. Hand probings an indicated by the prefix "H' CLASSIFICATION: Classification on kegs is made by inspection in accordance with the Unified Soils Classification System (tee attached chart) using visual -manual procedures unless noted otherwise. GROUND WATER: Observations were made at the tines indicated. ►rosity of soil strata, seasonal weather conditions, site topography. etc., may cause changes in the water levels if led on the logs. SAMPLING: All Nmpi are taken with the standard 2" O. D. solit•tube sampler, except where noted. TW indicates thin - well undisturbed temple. BPF: Numbs I idicaN blows per foot recorded in standard penetration salt, alto known as "N" value. The sampler is Nt 6" Into undisturbed soil below the hollow -sum suer. Driving resistances an then counted for second and third 6" incrienants and added to get OFF. Wisre they differ significantly, they we reported in the follawing form — 2112 for the second and third 6" incre rernts reepeetively. WH: WH wndicates that asmpler penetrated soil under weight of hemmer and rods alone, driving not required. NOTE: Ail tan run in scawdence with applicable ASTM stsndwdo. omen ENGINEERING TESTING 1 CL'.SSIFICATION OF SOILS FOR ENGINEERING PURPOSES ASTM DESIGNATION D-2487 1 Major Divisions N ^ M � V 4N Q Qp i ■ Z ,� to Ox0 L C N N w it= Ogg r N 4 Lu -V ,5;a aa$ e u0 $A i- Group Typical Symbols Names Classification Criteria Hell -graded gravels and Cu - 000 ID 14 Greater than 4 c ow gravel -sand mixtures, little or no fines (D a Ca ' Dla Between 1 and 3 N 3 Poorly graded gravels and rap ravel -sand mixtures, Not meeting both criter's for OW r little or no fines o e 511 g9 siravels gravel- It mixturres Atterbe limits plot below " line or Atterberg limits plot- �•• c GN man plasticity index ting in hatched area less than 4 are borderline b•�• t Clayey growls, gravel- a „�limits P o above A line and irinclassifications re- qug use of dual r OC sand -clay mixtures plasticity index 7 symbols �•a• greater than Cu - D80/D10 Greater than 6 g N Aell-yrated sands and SW gravelly sends, little or no fines (D)E Ca - Been 1 and 3 QN$ e N Din X Dgp 6 ZG^ Poorly sands and BP graded gravelly sands, little Not nesting both criteria for BW 4 or no fines N GZM Silty sands, sand -silt Atterbary limits plot below "A line or Atterborg limits plot- T eL W OIL BN mixtures plasticity index less ting in hatched area than 4 -are borderline clas- Clayey sands, sand -clay erg plot above A line and sifications requiring use of symbols N 0 BC mixtures greater titann4ax Inorganic silts, rock flour, silty or clayey AM fine sand Inorganic clays of ow 5- media plasticity, yrav- lZ ally clays, sandy c�ays, silty clays, lean clays Organic silts and organic OL silty clays of low plasticity Inorganic silts, micaceous 0 or diatomaceous silts, elastic silts Inorganic clays of high M plasticity, fat clays Organic clays of median OH to high plasticity 60 s0 1 40 .r 30 20 a 14 Plaetietiy chart For *low of fine- Qrat"d #Ot 1e and fine Jleotton of ooa ne-gmatned coils. AtterbaV unite pplotting in hatched area are borderitne el"eifteattane requiriv we of drei 40""to.* /{gwtim 0f A-1 PI - 0. ?a Q_ 20Cz , 0 0 10 20 30 40 50 60 70 80 90 100 Ltqui,d Uxdt nl organic soils Pt Peat, uwck dnd other H1 9 Y ►g highly organic soils Visual -manual identification onAun' ENGINEERING TESTING 11 Telephone 473.7357 CITY Of ORONO Post Office Box 66 • Crystal Bay, Minnesota 55323 • Municipal OfScaa On the North Shore o/ Lake Minnetonka February 14, 1978 Mr. James Olson A.onestroo, Rosene, Anderlik 6 Associates, Inc. 2335 Hwy 36 St. Paul, MN 55113 Dear Mr. Olson: Enclosed is a cod., of the Braun Engineering Report on soil borings and percolation tests for Lot 8, Block 1 of the Farview Addition. Please note that of 21 percolation tests performed, only 3 gave results of 60 mpi or less. Three possible systems have been roposed, including an osmosis system with which I am not familiar. riease review this report and recommend which system, if any, would be feasible for this lot. Thanks! Sincerely; 4'- Michael P: Gaffron Septic System Inspector 'LPG: sm Enclosure 8 A' Rom. 444d4 & 4. ,, 9,wr e� "is */. 16"A -44FAMOV d6 one 0. •eweeb", P.R. Lewrewer P. reYWw• ra. At Aa4 NAmoswls aa»a Robot Romm,dM0 reek, r.a. ph C. Jeeerk c. An4dtk, r.t P.R.Pir.Gig=X"A A. re�w �. r+,r,bA, Pi. P�nssv `-t �,tA^ WOMwV O Buller/ A. L nsbos P.F. the •�r.r, P.R. Reber D. PHONVI, Pi. Rk �n, rl. February 21, 1978 FED '2 Rk"erf X. rrrwer, P.E. JMWS C. otMw, P.H. Rubes d" rl. Afwvk, c..', *Id. r,s. 6 .q0 P.R. Ar~gk R. MN&W' r r. Mr. Michael P. Gaffro � A. zp kkwx "' � �R`- Septic System inspecto L"MHES M. Lee M. kky kp KWAM M. obew City of Orono Box 66 Crystal Bay, Mn. 55323 Re: Percolation Tests Lot 8, Block 1 Farview Addition Cur File No. 139 Lear M: , C 'iron: We have =.viewed the Soil Borings and Percolation Tests Report dated February 13, 1978 prepa�.ed by Braun Engineering Testing for the above lot. Based on the test resulca indicated in the report, a standard septic tank-drainfield system cannot .e apl,, wed. The tesz results exceed the minimum requirements by such a large de,yree gnat no further consideration should be given to the standard sys- tem. With respect to innovative systems, we quote from Section 4 of the proposed "City of Orono On -Site Sewage Treatment System Design Manual" as follows: "Application for innovative system installation variances shall include all the data required for standard system application, plus any addition- al data necessary to establish the acct�ptsbility of the proposal. Such data would normally include case histor, I similar installations, manufacturer's literature, independent results and engineering re- ports." The Braun report suggests that the mound system may be ieasible. However, no detailed design features or layouts are presented. The proposed On -Site Design Manual indicates that percolation rates should be faster than 60 minutes per inch on the surface and faster than 120 minutes per inch in the sub -soil and/or sub- stratuir for the mound system. We recommend that the Owner of Lot 8, Block 1 be advised that based on percola- tion rates submitted in the test data, the standard septic tank-drainfield sys- tem cannot be installed and further if he wishes to pursue any alternate innovative system, he must submit a detailed design layout in accordance with Section 4 listed above. The City of Orono should not be placed in the position of designing a system for the property owner, but rather should review a proposed design prepared for and submitted by the Owner. Page 1. Mr. Michael P. Gaffron City of Orono Crystal Bay, Mn. 55323 Re: Percolation Tests Our File No. 139 February 21, 1978 If tie may be of further as tace in this matter, please contact us at your con- venie� ,e. Y_aY., very truly, BONEST"G, ROSUNE, ANDERJIK & ASSOCIATES, INC.. J, C. Ols CO.li Page 2. �E je::Aroo*P Al i r2 —we— �A 005Vaviz ev c% 4/r at/O BLOCK l �� (ORoR�sED N(ouvo :��T�� I / ;✓`Q� OK I � i I � lomun'"', L�NauNEENIWri rEaTING ofes. L-c�7- 8i 5La,r / ��✓/��v d�rrr R9^10, M 1A/N. Z-ZZ- rn D 3 O c Z T s —a E-4 Y -4" STRAW OR MARSH HAY L SANDY LOAM SOIL GRASS COVER---,-- I V4" PERFORATED SAND FILL PIPE 6" TOPSOIL MAXIMUM SLOPE 3 TO 1 OP % SLOPE SU PLOWED OR DISKED SURFACE 3/4' - 2 1/2" CLEAN ROCK CROSS SECTION A - A 1 1/2"- 2" PIPE FROM PUMPING CHAMBER FTTTA\-TT-11 I V4" PERFORATED PIPE BED AREA *4 "- 2 1/2" - CLEAN ROCK J z w J 0 w cn DIKEIN 1. 10' MAX DIKE —TOTAL WIDTH PLAN VIEW SEWAGE TREATMENT MOUND WITH PRESSURE DISTRIBUTION OF EFFLUENT Telephone 473-7357 CITY of ORONO Pat Once Box 66 • Crystal Bay, Minnesota SM23 • Municipal Office* On the North Shore of Lake Minnetonka February 27, 1978 Mr. Jim Olson Bonestroo, Rosene, Anderlik & Associates, Inc. 2335 Highway 36 St. Paul, MN 55113 Dear Jim: Mr. Scott Abernathy, of David Nitz, Inc., has or will soon deliver to you plans for a proposed drainfield for Lot 8, Block 1, Farview Addition, incorporating a Mound treatment system. I believe you already have the Braun Engineering report including perc tests for this lot. Please review these plans and make a recommendation as to approval or denial of this system. Thank you. Sincerely, Michael P. Gaffron Septic System Inspector MPG: sm