HomeMy WebLinkAbout1987-01-12 Site Evaluation ReportHakanson
Anderson
As-, :., Inc.
January 12, 1987
Mr. David Nitz
950 Red Sandstone Road, #41
Vail, CO 81658
Dear Mr. Nitz:
Enoneers, Surw pots &
Landscape Archk cis
At your request a site evaluation to determine soil suitability for
an on -site sewage treatment system was performed at Lot 12, Block
1, Farview in the City of Orono, Minnesota. Standard methods of
percolation testing were employed. Elevations are relative to an
assumed elevation of 104.0 based at a double spike in a birch tree
near the southwest property corner as set by Strgar-Roscoe-Fausch
Inc. (see enclosed sketch).
This report includes:
1. Soil boring logs
2. Percolation test results
3. Testhole location and septic system configuration sketch
4. Septic system design specifications
5. Discussion and recommendations.
The soil boring logs show that sandy loam to sandy clay loam
surface soils overlie sandy clay loam to clay subsur-face soil
horizons. Soil mottling begins at 2.0 ti 2.5 feet depth at the
b,�reholes. Soil mottl,2s (spots of contrasting color) are accepted
indicators of periodic saturation in soils. Gleying begins at 2.0
to 5.0 feet depth at the bcreholes. Gleying (dull gray soil color)
forms in soils which are saturated and Ln a chemically reduced
condition for long periods of time. Ground water was at elevation
94.1 to 94.8 at the boreholts or Tanuary 9, 1987.
Percolation test results are as follows:
Hole Elevation Depth (inches)
Soil Texture at
Bottom cf Hole
Percolation Rate
min ink_
P-1
98.4
24
Sandy
loam
3
P-2
98.1
24
Sandy
loam
to sandy 9
clay
loam
P-3
96.6
18
Sandy
clay
loam 5
P-4
95.8
18
Sandy
clay
loam 8
P-5
98.6
24
Sandy
cl--y
loam 5
P-6
96.8
24
Sandy
clay
loam 6
222 Monroe Street Eugene 1. Hakanson. PL
Anoka. Minnesota 55303 James M. Wlnter. L.S.
Lawrence G. Koshak, PL
612/427-5860 Peter R Raadkka. PE..
Mr. David Nitz
Pag s 2
January 12, 1987
Measured percolation rates are consistent to somewhat rapid for the
texture of the soil materials in which the percolation tests were
run.
The City of Orono requires at least three feet elevation difference
between the bottom of the filter rock of a septic system and ground
water or indication of periodic soil saturation such as soil
mottling. To meet this requirement, a mound septic system is
recommended for the primary and secondary septic systems at this
site.
The mound is designed to serve a four bedroom house with a
whirlpool bath. Design sewage flow for the house is 600 gallons
per day. A sewage flow of 100 gallons per day is added for the
whirlpool bath. Total design sewage flow is 700 gallons per day.
with a design infiltration rate of 1.2 gallons effluent per square
foot per day for the medium sand fill material of the mound, the
required rock bed area of the mound is 700 square feet.
700 gal/day 1.2 gal/ft2/day = 583 ft2
A rock bed 10.0 feet wide by 60.0 feet long provides the needed
area. A minimum of one foot (1.01) of medium sand should be
constructed below the rock bed.
The pressure distribution system of the mound consists of Schec _e
40 PVC plastic pipe. The supply pipe should slope back towards the
pumping chamber so that it drains after the mound is dosed. The
la::ezals are 1.5 inch inside diamete- r-pes. The laterals should
have 1/4 inch diameter holes drilled at a spacing of 3.0 feet. The
laterals should be assembled to the manifold so that the holes
point downwards into the rock bed. The distal ends of the laterals
should be drilled norizontally in the end cap near the crown of the
pipe to facilitate air venting.
A submersible effluent pump capable c•f deliver.Lng at least 45
gallons per minute against a total dynamic head of at least 10.2
feet should be selected. Headlosse- are calculated as follows:
1. Verti.:al headloss of 4.5 feet between pump disc,arge (approx.
elev. 95.0) and manifold (approx. elev. 99.5),
i�tion �oss of 0.7 feet in 20 feet of supply pipe (3.3 feet
per 100 feet 2.0 inch I.D. plastic pipe at 45 gpm flow),
3. Five feet (5.01) to account for losses in distribution network.
M. David Nitz
Page 3
January 12, 1987
If as -built elevations are different from those above, headloss
should be recalculated to ensure proper pump selection.
The pump should be rigged with mercury float switches to dose about
175 gallons of effluent to the mound. An additional mercury float
switch should be installed on a separate circuit to an alarm device
to warn of failure. The mercury switches should be rigged to allow
700 gallons reserve capacity in the pumping chamber. All
electrical connections should be watertight.
The septic tanks should each have at least 1,000 gallons capacity.
The pumping chamber should have at least 1,000 gallons capacity.
It is recommended that a water meter be installed to monitor water
use. Exterior sillcocks should be excluded from the metered water
system. The water meter should be read periodically and water use
patterns adjusted if necessary to ensure that the design sewage
flow of the septic system is not exceeded.
The area for the proposed primary septic system should be roped off
to prevent vehicular traffic on the site. Construction of the
mound system should begin only when the moisture content of the
topsoil is lower than the plastic limit.
It is highly recommended that the installer of this septic system
holds an Individual Sewage Treatment Systems Certificate for
installation issued by the Minnesota Pollution Control Agency.
The sole purpose of soils data contained herein is evaluation of
soil suitability for on-ait,�t absorption of septic tank effluent at
the test site. AlthOlAgh so'_1 texture and horizonation information
and groundwater elevation data may be helpful for the setting of
basement elevations at this site, we cannot warrant any such inter-
pretations or use of this c.ata for other purposes.
If you have any questions about information contained in this
report, please feel free to contact me.
Sincerely,
HAKANSON ANDERSON ASSOCIATES, INC.
. Aa, " If. ( /" <- - - - - - "
Gary J. thbun, Soil Scientist
Enclosures
File: 1540.07
PMWT: Nitz Site
Evaluation
FILE No.
1540.01
BMING ItM: 4" Flight
Auger
WE:
1/9/87
(feet) 0.0 ark brown sandyloam----
Dark grayish brown sandy loam
o sandy clay loam
,rayish brown sandy clay, few
o many yellowish brown
ttles with depth, few to
ny gray gleyed areas
/depth
I
END OF BORING
1.1
2A
7.(
Borehole i 1
FI NaTtnu - aA
*Ground water at 94.8 on 1/9/87
WAM NCUSM ASSOCIATES, INC.
AP
3.0
5.0
7.5
Borehole / 2
rk
brown to ac c san y
lay
loam, moist to wet
ith
depth
Dark
grayish brown sandy clay
loam
Gray
clay, many yellowish
brown mottles
Grayish brown sandy clay,
many
red mottles, many gray
gleyed areas
END OF BORING
*Ground water at 94.4 on 1/9/87
BY: ,� 1
PfVjECT; Ni tz Site Evaluation RLE No. 1540.01
BORIM MEhw: 4" Flight Auger DOE: 1/9/87
DfeDEPTH 0. 0
1.0
1.5
2.5
4.0
991
Borehole / 3
FI LVATf nu - 07 C
ark brown sandy loam to sand
lay loam
Grayish brown sandy loam to
sandy clay loam
Brown sandy clay loam
Grayish brown sandy clay.
many yellowish brown mottles,
many gray gleyed area,, wet
Grayish brown sandy silt,
many yellowish brown mottles,
many gray gleyed areas, wet
Grayish brown sandy clay,
many yellowish brown mottles,
many gray gleyed areas
END OF BORING
roundat 94.1 on
O`1 >I T�• �•�
.r
"ee
Borehole i
.