HomeMy WebLinkAbout1994-10-26 Soil Test ReportBRAUN'
I NTE RTEC
October 26, 1994
Ms. Teresa Whaley
Home Reflections
1340 Phillips Drive
Long Lake, MN 55356
Dear Ms. Whaley:
,7 1994
.,�, tt,r.,,.� ca,p„amiw
6801 Washington Avenue South
P.O. Box 39108
Minneapolis, Minnaola 554394108
612.941.5600 Fax: 941.4151
Engineers and Scientists Serving
the Built and Natural Environments`
Project BABX-94-463
Re: Excavation Observations and Compaction Testing, Proposed House at 1090 Cox Farm
Road, Shadowwood Subdivision, Orono, Minnesota
As you authorized on June 28, 1994, we have performed excavation observations and
compaction testing during pad preparation for a house pad in the Shadowwood subdivision in
Orono. The purpose of the observations was to assist in determining the suitability of site soils
for support of a proposed house and attached garage. The purpose of our compaction testing
was to assist in evaluating the compacted density of fill placed below footings.
Proposed Construction
We understand the house will have a full basement with a walkout. The garage is located along
the west side. We understand the house will be of mostly wood -frame construction, and have
assumed foundation bearing pressures will not exceed 2,500 pounds per square foot.
Excavation Observations
Observations were performed on June 28 and 29 and July 1, 1994. At the time of the initial
observation, the house pad had been excavated to roughly the proposed footing grades.
As part of the observations, hand auger probes to depths of about 3 to 4 feet below the
excavation bottoms were performed. Estimates of soil consistency were made based on the
force required to advance the auger. Classifications were determined in general accordance
with American Society for Testing and Materials (ASTM) procedures by examining the auger
cuttings.
Initial observation consisted of hand auger borings and two test pits. The test pits were
excavated and observed outside of the limits of the proposed house pad. Results of the test pit
observations and hand auger borings indicated that existing soils at proposed footing elevations
were not suitable for support of the proposed house and garage without incurring an
Home Reflections
Project BABX-94-463
October 26, 1994
Page 2
unacceptably high risk of structural distress due to differential settlement. We recommended
the disturbed, soft or loose sands, silts and clays be excavated and replaced with engineered
backfill to provide a pad suitable for support of the house and garage. We also recommended a
smooth -bucket backhoe perform the excavating in order to minimize further disturbance of the
underlying natural but saturated soils.
Excavation to suitable soils was performed on July 1, 1994. Unsuitable soils were excavated to
depth from about 5 to 10 feet below existing site grades. Based on information we were
provided, this elevation was about 5 feet below the proposed basement footing elevation.
After unsuitable soils were excavated, the bottom soil observed was sandy lean clay glacial till
judged to be medium to rather stiff in consistency.
A minimum of 10 feet of excavation oversizing was provided beyond the proposed outside
edges of perimeter footings. Excavation oversizing was judged adequate.
Compaction Testing
Four compaction tests were performed in compacted backfill. Soil used as backfill was
imported poorly graded sand with silt. It was compacted using a smooth -drum roller. Results
of all compaction tests exceeded the recommended minimum of 95 percent of the maximum dry
density determined in accordance with ASTM Test Method D 698 (standard Proctor).
Compaction and Proctor test results are attached.
Conclusions
Our conclusions are based on the results of our excavation observations and compaction testing,
and information we were provided regarding the proposed construction. Based on this, it is our
opinion excavation bottom soils observed are suitable for support of backfill and the proposed
construction. It is also our opinion that adequate excavation oversizirg was provided.
Based on compaction test results, it is our opinion backfills were compacted to densities
exceeding the recommended minimum of 95 percent of standard Proctor density at the locations
and elevations of the tests.
General
Standard penetration test borings with power equipment were not authorized nor taken in the
building area to evaluate the soils at depth. However, the soils which were visible and the
Home Reflections
Project BABX-94-463
October 26, 1994
Page 3
results of the hand auger probes indicate that the risk of detrimental settlement due to poor soils
at depth is small and we thus recommend it be assumed by the owner.
Services performed by Braun Intertec for this project have been conducted with that level of
care and skill ordinarily exercised by members of the profession currently practicing in this
area under similar budget and time restraints. No warranty, expressed or implied, is made.
It has been a pleasure providing our services for you. If you have any questions, please call
Greg Glitto at (612) 942.4841.
Sincerely,
p
U�
4i6—
Gregory J. Glitto
Staff Engineer
Professional Certification
I hereby certify that this report was prepared under my
direct supervision and that I am a duly Registered
Professional Engineer under the laws of the State of
Minnesota.
LL\/,-//21
. Braun, PE
Senior Engineer
Registration Number: 14969
Attachments:
Reports of Field Compaction Tests 1 through 4
Proctor P-1
c: Mr. Bruce Vang
City of Orono
drt\&\Iwb: mjz%ab x\94463 \obupt
BRAUN sm
I NTE RTEC
Report of Field Compaction Tests
Date: July 12, 1994
Client:
Ms. Teresa Whaley
Home Reflections
1340 Phillips Drive
koun h- ma floc CwporeMon
6801 Washington Avenue South
P.O. Box 39108
Minneapolis, Minnesota 55439-0108
612.941.5600 Fax: 941.4151
Engineers and Scientists Serving
the Built and Natural Environments
Project: BABX-94-463 Report: I
Project Description:
County Road 6 and Willow
Shadowood Subdivision
Orono, Minnesota
ayss
Test
L4AY, 1.{11
Date
✓✓✓✓v
Type
Soil
ID and
Classification
Optimum
Moisture*
M
Max. Lab
Dry Density*
(Std.Proc.)
(pct)
Inplace
Moisture
M
Inplace
Dry
Density
(pcf)
Relative
Compaction
M
Specified
Minimum
Compact.
M
Comments
1
7/6/94
N
P-1: SP -SM
14.5
109.5
11
118
108
95
A
2
7/6/94
N
P-1: SP -SM
14.5
109.5
7
113
103
95
A
3
7/6/94
N
P-1: SP -SM
14.5
109.5
6
112
102
95
A
4
1 7/6/94
N
P-1: SP -SM
14.5
109.5
6
113
103
95
A
Key: N = Nuclear, ASTM D 2922 A = Test results comply with specifications.
SC = Sand Cone, ASTM D 1556 B = Test results do not comply with specifications.
* = O.M. and M.L.D.D. rounded to nearest 0.5
Test
Test Location
Elevation
1 38'S,
56'E of NW House Pad Corner
99
2 12'S,
48'E of NW House Pad Corner
98'h
3 35'S,
15'E of NW House Pad Corner
99
4 15'S,
2'E of NW House Pad Corner
98
Elevation Reference: Assumed elevation of bottom of basement footing = 100.
cc: Mr. Bruce Vang
City of Orono
mkm\babx\94463\ct. l
Braun Intertec Corporation
.1� Az
Daniel R. Burns, PE
Project Engineer
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Date,.
As Received,
Preparation
Rammer
Depth
Tested
Size of Percent
Percent Percent
I Percent Natural
Specific
Oversize Oversize
on 3/4 3/4 to 3/8
3/8 to 44 Moisture
Gravity
TEST RESULTS
MATERIAL
Maximum dry density - 109.5 PCf
SP—SM Poorly Graded Sand
moisture - 14.5 %
w/silt fine grain, brown
_____O_ptimum
Proje=t No.: BABSubdivision
Orono, Minnesota
assumed.
Date:Location:
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