HomeMy WebLinkAbout1988-10-05 Soil Compaction Test ReportAs authorized by you on September 15, 1988, we have
completed an excavation observation and performed compaction
testing at the above referenced site.
The observation was performed on September 15, 1988, by a
certified engineering technician. The compaction tests were
performed in fill soils placed on September 15 and 16, 1988.
BACKGROUND
A proposed single-family home is planned for this lot. From
a site plan prepared by Sathre-Berquist, Inc., it was indi-
cated that the garage slab will be placed at an elevation of
1024+. The lowest floor will be placed at an elevation of
1012+. The east 50+ feet of the home will be at the pro-
posed walk -out elevation of 1012+. The remainder of the
house and the garage will have a slab -on -grade elevation of
approximately 1024+.
C7
I
Ouer�ry Semce. S,nce 1957
F-RAUR'
COEOTECNSUL
�>rla
INEERING TESTING
�M
NICALING
AND MATT
GEOTECHNICAL AND MATERIALS
No
St Oo
ROOY b Wd'"610 m
axnt+a
SI Peal
P.O. Box 35108
Mpls., MN 55435
AFTWTE10Nnc
(612) 941-5600
MOM Moho
9 'k
FAX /941-4151
warlwn
MEW
October 5, 1988
Ulm
a.�ew
Cm mG4w PE
P&4" AM— E
Landform, Inc.
a..aala,a,PE
Ebp„ v Bo�q.+I P.0
Attn: Mr. Al Musech
°E
80 West 78th Street_
e",""a',�°„"r�
wmuW� nrE
Chanhassen, MN 55317
IMmxa Bw P
14h,e14 Hte, PE
,
°f",
RE: 88-609 EXCAVATION OBSERVATION
WA Ia ��FPF
AND COMPACTION TESTING
Proposed Home
wEunE�tora�E
i
4165 Bay Side Road
unwnan K
l�nn P,.,nrM
Orono, Minnesota
1 I�tMnbeet k
Dear Mr. Musech:
As authorized by you on September 15, 1988, we have
completed an excavation observation and performed compaction
testing at the above referenced site.
The observation was performed on September 15, 1988, by a
certified engineering technician. The compaction tests were
performed in fill soils placed on September 15 and 16, 1988.
BACKGROUND
A proposed single-family home is planned for this lot. From
a site plan prepared by Sathre-Berquist, Inc., it was indi-
cated that the garage slab will be placed at an elevation of
1024+. The lowest floor will be placed at an elevation of
1012+. The east 50+ feet of the home will be at the pro-
posed walk -out elevation of 1012+. The remainder of the
house and the garage will have a slab -on -grade elevation of
approximately 1024+.
C7
I
88-609 _2_ Dctnber 5, 1989
Landform, Inc.
After the excavation tractor excavated the level
7•++rr of
the proposed home, a. Ori in the elevations .».s found.
The excavation was
apt x u,, -el y 3 feet lower t~r,ximatelye3
on the plan. This r iced proposed
eme lan eleof vation.
feet of soil to reatt the proposed p
EXCAVATION OBSEF.VATIO.
;,t the time of the ervation, a bulldozer had removed
soils in the area of nroposed lower tnatelye 2 to home.
On the south side of ]come, app
in
soil had beenremoved. Nextto therom the lower mmon evelwrequiredratcut
the slab -on -grade area
of approximately 10 fee..
y 2 to 3 feet larger than the
The excavation was apprcc etel
prosouth of
posed area of the i0�e. The excavation limits were
locatedfromsoutheast an offset . building c,r er that Was set 15 feet
the
e of the
The was at bottom Of eThisa elevation txcavtion at hewasmdeterminedb with observation
excavation contractor's survey instrument and level d
The bench mark used was the stake at the northwest garage
corner. An assumed elevation of 1024.5 was assigned to this
location. d in
ils be
ace
and uniformly recommended backfill
We c the mpactedwith aovibr torylcompactor.hin lifts
COMPACTION TESTING
Three compaction tests were taken on September 15, 1988.
the
The testsnot meet
id
requirementdof 95% f standards Proctord density. compaction
mended the area be recompacted and retested.
to bly
The techniciAn wpv-, re rested Theearchitecton siteawfoot. Thin ai5 on xsiteeat
9:30 a.m. cn a u:•s indicated that the floor grade in the
that time. t.
vat oflowered 1
u1 foot ofufillethat was placed on September 15.
remo-
a after th
rT.11ac. technician was moval of the 1 footeofesoil,tan3 he areao retest ewas erecompactede
Awk
r
88-609
Landform, inc.
October 5, 1988
the afternoon of September 16.
Retests were taken reviously taken
Because two of these faction tests were Ps at approxima-
at elevation 1014 and a new^floor
one retest were `aken at
tely 1013, two additio ,,tion tests met or exceeded the
elevation 1013. These c' P irements of 95% of standard
Specified minimum comp -is, requ
Proctor density.
Soils placed at a minima ` 95*~ of standard Proctor proosior-
ara suitable for support c typical spreadCessure9 of 2,000
tinned to exert a maximi :oil bearing p
pounds per square foot.
CONC 'IONS
Based on our excavation -beervation and compaction test
result, iis Oured in the
bottoms of tthe excavoatioh cdatthe ®fill l so lserplac d are
suitable for support of t proposed footing and/or foun-
dation loads.
GENERAL REMARKS
It should be noted that standard penetration test borings
with power equipmentthe were
soils takento
were visible the
soiland sthe
at
depth. Howeverr,,
results of the hand auger probes indicate soils at that
depth issvery
detrimental settlement due to p
small and we, thus, recommend that it be assumed by the
owner. The cost for taking arranted borings to better define
that risk does not app
Services performed by the geotechnical engineers for this
project have been conducted in a manner consistent with that
level members of
ordinarily
currently practicing in exercised
thisdare
theca. This is
our professional responsibility. No warranty, expressed or
implied, is made.
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REPORT OF FIELD
COMPACTION TESTS
i ■IIIMFEOTa-Minneapolis. Mlohmg SI cloud Rochester sl Paul
a.rrly tu: P.O. Box 35108
Minneapolis, MN 55435
Client:
Landform Inc.
Attn: Mr. Al Musech
80 M. 78th St.
Chanhassen, MN 65317
emon" Ouenry Serraoa 9rrce t957
ENGINEERING TESTING
uw t>AtK
September 20, 1988
Date: t
Project a: 88-609 Report a: 1
Project Description: Exc. Obs 8 Cts.
Single Family Dwell.
4165 Bayside Rd.
Orono, MN
TMl
Not
I D
ogv.r.m
Mp1tW.IPCF)
w. Lae
Dry D..wry
M Pu -
%U-Nre
In Fyt.
D$v D—slyG+lvI.ulM
IecFl1
42'N, 14111 of
SE
building
P-1
SC
16.5
112.8
I1.7
94.1
83542
1014
3
P-1
SC
16.5
112.8
11.9
100.9
8954 95
1-B'
3
9/15/88 P-1
Sc
16.5
112.8
11.3
106.3
94 95
I 1-8"
4
9/16/88 P-1
Sc
16.5
112.8
9.1
115.9
102 95
1-A
5
9/16/88 P-1
Sc
16.5
112.8
8.8
110.1
9754 95
1-A
IA
9/16/88 P-1
Sc
16.5
112.8
11.5
110.8
9B 95
1-A
nuclear Method ASTM: 02922-81 —1L Standard Proctor ASTM D698-78
_X Sand Cone Melhod ASTM: D1556-82 Modified Proctor ASTM D1557-78
Bench Mark: Basement grade 1013
leu
No
,EST LOCatION
E1 -1—
I
42'N, 14111 of
SE
building
corner
1013
2
21% 141W of
SE
building
corner
1014
3
21'N, 37'W of
SE
building
corner
1014
4
25'N, 201W of
SE
building
corner
1013
5
25'N, 38'W of
SE
building
corner
1013
IA
RETEST
1013
n
were removed.
wa w re
o e eva on1J Solis ror tests z and 3
1. Fill A. Test Results Comply With Specifications. Respectfully Submd:ed.
2. B. Test Resulls Do Not Comply With Specifications. Braun Engineering Testing Inc.
NOTES: % n / /�
cc: lT" A
Ronald R. Urbach
C:88609-1/ijm Certified Engineering Technician
L
Mr. Jame:: Alt
May 19, 1988
Page 2
The measured percolation rates are consistent with the texture of
the soil materials in which the percolation tests were run.
Septic system drainfields require at least three (3.0) feet eleva-
tion difference between the bottom of the filter rock and ground
water or indication of periodic soil satura':ion such as soil mott-
ling to perform properly. To meet this requirement, a mound septic
system is recommended for soil conditions on this lot.
The mound is designed to serve a four bedroom house with a whirl-
pool bath. Design sewage flow is 600 gallons per day for the
house. A sewage flow of 75 gallons per day is added for the
whirlpool bath. Total design -ewage flow is 675 square feet. With
a design infiltration rate of 1.2 gallons effluent per square foot
per day, the required rock bed area of the mound is 562.5 square
feet.
675 gal/day - 1.2 gal/ft 2/day - 562.5 ft
A rock bed 10.0 feet wide by 56.0 feet long provides the needed
area. A minimum of one (1.01) foot of medium sand should be con-
structed below the rock bed of the mound.
The pressure distribution system of the mound consists of Schedule
40 PVC plastic pipe. The supply pipe should slope back towards the
Pumping chamber so that it drains after the mourd is dosed. The
laterals are 1.5 inch inside diameter pipes. The laterals should
have 1/4 inch diameter holes drilled at a spacing of 7.0 feet. The
laterals should be assembled to the manifold so that the holes
point downwards into the rock bed. The C stal ends of the laterals
should be drilled horizontally in the end cap near the crown of the
pipe to facilitate air venting.
A submersible effluent pump capable of delivering at least 42
gallons per minute against a total dynamic head of at least 22.7
feet should be selected. Headlosses are calculated as follows:
1. Vertical headloss of 12.2 feet between pump di.:harge (approx.
elev. 87.0) and manifold (approx. elev. 99.2)
2. Friction loss of 4.1 feet in 14C feet of supply pipe (2.9 feet
per 100 feet 2.0 inch inch I.D. plastic pipe at 42 gpm flow),
3. Friction loss of 1.0 feet in piee fittings equal to 25 percent
of friction loss in supply pipe.
4. Five feet (5.01) to account for losses in distribution network.
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{{� Mr. James Alt
May 19, 1988
J Page Three
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If as -built elevations are different from those above, headloss
should be recalculated to ensure proper pump selection.
The pump should be rigged with mercury float switches to dose about
170 gallons of effluent to the mound. An additional mercury float
switch should be installed on a separate circuit to an alarm device
to warn of pump failure. The mercury switches should be rigged to
allow 675 gallons reserve capacity :n the pumping chamber. All
electrical connections should be watertight.
The two septic tanks should have at least 1,000 gallons capacity
each. The pumping chamber should have at least 1,000 gallons
capacity.
It is recommended that a water meter be installed to monitor water
use. The meter should be hooked to the water system such that
exterior sillcocks are excluded. The water meter should be read
periodically to ensure that the design capacity of the septic
j system is not exceeded.
1 It is highly recommende2 that the installer of this septic system
1 holds an Individual Sewage Treatment Systems Certificate for
installation issued by zhe Minnesota Pollution Control Agency.
The sole purpose of soils data costa'-ned herein is evaluation of
soil suitability for on-site absorc=ion cf septic tank effluent at
the test site. Although soil text_re and horizonation information
and groundwater elevation data may 'e helpful for the setting of
basement elevations at this site, we cannot warrant any such inter-
pretations or use of this data for ether purposes.
If you have any questions about infcrzaticn contained in this
report, please feel free to contact me.
Sincerely,
HAKANSON ANDERSON ASSOCIATES, INC.
, < �_/" . (. nom« I
Gary J. hbun, Soil Scientist
/ckl
Enclosures
i
File: 1788.01
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LUL OF SOIL BORIN-:S
PRWECT; Alt Site Evaluation FILE No. 1788.01
BRING PIETHOD; 4" Flight Auger DATE; 5/18/88
Borehole 01 Borehole hZ
Q 'H - 96.1 DEPTH
(fee C) 0.0 - 96 4
Dark bran, silt loam (feet)O•
1. 1.
Grayish brown silt loam
1.5 I
Brown silty clay loam
2.0
Grayish brown sandy clay, 2.
few yellowish brown d gray ctles
2.
Grayish brown sandy clay.
many yellowish brown 6 gray
mottles
5.
Grayish brown silty medium
to coarse sand
6.
Grayish brown silty clay,
many yellowish brown 6 Gray
mottles
7.
END OF BORING
Ground water not encountered
WifcANSOI NUM ASSOCIATES. INC.
•
M
0
Dark brmn silt loam
0
Dari: grayish brown silt
i
lQam
Brown silty clay loam
0 —
Brown clay loam, few yellowi
brown 6 gray mottles
0
Grayish brown sandy clay,
many yellowish brown 6 gray
mottles
Grayish brown silty clay,
many yellowish brown 6
Fray outtles
END OF BCPTNG
Ground water not encountered
BY ,—
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�M.
-01
UM OF SOIL BORI L
PROJECT: Alt Site Evaluation FILE NO, 1788.01
BORING PtTHOD; 4" Flight Auger DATE: 5/18/88
Borehole it Borehole F1
!CPTH ELFVATION - 96.1 DEPTH
0.0 Dark brovu silt loam (feet)0-
1.0 1. 1.
Grayish brown silt loam
Brown silty clay loam
2.0
Grayish brawn sandy clI
..
few yellowish brown 6 tales
1.
Grayish brown sandy cl
many yellowish brown 6
mottles
5. ..f
Grayish brown silty medlunr.
to coarse sanu
6. _
Crayish brown silty clay,
many yellowish brown 6 Gray
mottles
1.
END OF BORING
Ground water not encountered
WWINSON A EEWI ASSOCIATES, INC.
W
0
Dark brown silt loam
0 -
Dark grayish brown silt
Brown silty clay loam
0
Brown clay loam, few yellowl
brown 6 gray mottles
Grayish brown sandy clay,
many yellowish brown 6 gray
mottles
Grayish bro-:n silty clay,
many yellwish brown 6
gray muttles
END OF BORING
Ground water not encountered
1
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_._.ft
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1 LOGS OF SOIL 0"i"-
PROJECT:
nn"i"-PROJECT: Alt site evaluation 1788.01
BORING METHOD: 4" Flight Auger 5/18/88
3
d
Barehole 05 Borehole V6
DEPTH - 98.0 DEPTH FIFVATIoN - 96.4
(feet) 0.0
1.
2.0
3.
Dark brown silt loam
Grayish brown silt loam
to silty clay loam
Grayish brown silty clay
loam, few yellowish brown
and gray mottles
Grayish brain sandy clay,
many yellowish brown 6
gray mottles
END OF BORI�NG
Ground water not encounterea
HAKAIISON AICERSUI ASSOCIATES. INC.
(fee,'-.:
FEND OF BORING
I
c__nd water not encountered
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