HomeMy WebLinkAbout12-22-1988 Soil Test Report Pg2 of 3662 CROMWELL AVENUE
ST. PAUL. MN 55114
PHONE 612/645-3601
SQlUBSERVAnCN$.aiILlESTlll5
LABORATORY No. 4220 89>464
December 22* 1968
2
one»ha1f stcries above the existing grade. The addition xill be 19* wide by 24' long
with a floor slab elevation matching the existing slab elevation of the lower floor of
the existing house. The addition will be supported on e perin«ter strip footing
approximately 2* in width. We have not been provided with the soil bearing pressures
from the proposed project* but we assume they will be on the order of 150C to 2000 psf.
Tc our knowledge* no deep soil test borings were performed for this project.
Accordingly* we cannot comment on the soil conditions beneath the depths of our shallow
hand auger borings.
CBSEWATION ICTWODS AMD RESULTS
On November 10* 1988* we visited the site at the contractors request to review the soils
exposed in the perimeter footing trench excavations. Our observation methods included
observing the sides of the excavation* placing shallow hand auger borings within the
exposed excavation bottoms and classifying the retrieved soils according to ASTN:D2488.
In addition* estimates were made of the strength properties of the retrieved soils.
In the majority of the footing excavations* the surficial topsoil and any soft fill soils
appeared to have been adequately removed. The soils exposed at planned bottom of footing
elevation typically consisted of stiff sandy lean clay* or medium dense clayey sand and
silty sand. We also observed that the perimeter footing excavaticr. matched the bottom of
the existing building at the southeast addition corner and was approximately 2' below the
existing footing elevation at the southwest building corner. The soils observed in the
excavations appeared to be naturally occurring glacial till* and were judged suitable for
support of assumed loadings of 1500 to 2000 psf.
The exception to the above noted soil conditions occurred at two locations. A1 a point
approximately 8* west of the southeast corner of the addition* the footing line
intersected the existing sanitary sewer pipe for the residence. We recommended that
approximately 2' of additional excavation be performed in this area to allow the new
footing to step under the existing sewer pipe. Based on our hand auger borings* it
appeared that soils exposed at the bottom of this additional 2* cut would be suitable
naturally cccurring soils similar to the majority of the footing areas. At a point near
•liie southwest corner of the proposed addition area* the footing trench again intersected
the fill soils from an existing utility line in this area. This previous trench appeared
to be approximately 1' wide and 2' to 3* deep. In this area* the contractor elected to
construct a small grade beam to span over the existing utility trench fill soils and
allow the footing loads in this area to be carried by the more competent natural soils
encountered on either side of the trench. It appeared that the natural soils on either
side of the trench would be suitable for support of the additicnal loads transmitted from
the grade beam to the foundation elements.
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