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X 1 0 : ^ -4 <br />1 ^ <br />BONESTROO <br />Ir. 0 0 >- <br />SOCX^^TES R . <br />Bonestroo <br />ffg la <br />Anderlik & <br />Associates <br />Engineers & Architects <br />January 7, 1994 <br />• lltTn.Hr A^rvn M find A li I*II 1*1 <br />Vet* A ff J ^yni* Pk 1 1*1 <br />C 1*1 Ih40^* ^ IVrteflr. PI thO*nj\ W Pf 1 pf <br />.M.HVWI 1 ^irvjU r|W 1’C^CK Ff .V«Hrwe«C lyrcaM l»*ff <br />I)#v«in lewiu. fC Jjmtl « f f 1 Ptu iiiyn* r| <br />♦.ITfWl M C-**** f't r.AIA 0 feiUHh PI Knii V Y.,^. t*r <br />Nufr-k 1*1 •«rr A |li4tftjLAI. fl Von J Ar^ri PI I>»iiAi*. * iv*<^ i*t <br />Marl A MjiMifi. Pf 1 • t PI <br />'■lUn .M Mv*rlai i i*a Vi t P.xjtmjr.*. rt « it#v pf Cr« III • -pf <br />fed r 1 rill PP U#1i A PI P#«i< r. 1p| <br />Itii4iwi* P AnrlrfWt.AlA Cwy w Miinrf« PI ItJftt 1' 1 <br />DjniH J PI I ll.UIP^ A J ,4 Ivwi <br />1 A»%pt\A t«U Pf IfiiM <br />PA.ty J Cr.^ Pf 1 L«il.lil M » 1-4 •» <br />r I m Utif 0 n 1 1 i <br />Ms. Jeanne A. Mabusth, <br />Building and Zoning Administrator <br />City of Orono <br />Post Office Box 66 <br />Crystal Bay, Minnesota 55323 <br />Re: ITiree Star Trucking Subdivision <br />File No. 139-1843 <br />Dear Jeanne, <br />We have reviewed the revised preliminaiy jilal and grading plan, and runoff/ponding <br />calculations submitted for the Three Star Trucking subdivision located north of Watertown <br />Road in the Southeast Quarter of the Southca.st Quarter of Section 33. We recommend <br />several modifications to the plan and calculntion.s. <br />As noted in our previous letter dated September 12, 1993, the drainage swale on Lot I must <br />be lowered to control the runoff within the subdivision. This change should be shown on <br />the grading plan. <br />The drainage for this property is an important issue due to the fact that much of the runoff <br />currently drains easterly through the developed properties in the Daniels Long Lake Heights <br />Addition. We recommend tJiat additional storage volume be provided in the pond on Lot <br />4 to reduce the outlet flows. Both the pond bottom and outlet could be lowered up to two <br />feet if the culvert is extended to the cast. Also, the easterly property, existing drainage <br />swale and existing culverts must be further investigated to determine the drainage capacity <br />available downstream. Tlie e.xisting drainage swale and culverts may need to be improved <br />at this time to prevent future property damage downstream. Further, we recommend that <br />the City obtain a drainage easement over the swale. This easement should be either <br />granted to the City or purchased by the developer. Tlicsc property owners should be <br />contacted to discuss the project. <br />A large portion of the pond on Lot 4 is shown within the wooden area. These trees will <br />need to be removed unless the pond location i.s changed. The pond outlet that consists of <br />both a 15 inch and a 36 inch culvert i.s acceptable, however, no detail has been provided that <br />shows the downstream end. Tlic elevated 36 inch culvert will create a high potential for <br />erosion and we recommend a drop manhole structure be added for control. <br />The septic sites, house site and pond shown on Lot 4 may be rearranged if necessary to save <br />the wooded area, however, testing for additional septic sites will need to be delayed