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04-16-1984 Planning Packet
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04-16-1984 Planning Packet
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, cul de sacs <br />be graveled <br />sements. <br />uts § $200). <br />roughout the <br />;^e covered or <br />» road <br />tad showing a <br />TO: <br />FROM: <br />DATE: <br />Jeanne A. Mabusth, Zoning Administrator <br />Michael P. Gaffron, Assistant Zoning Administrator <br />April 12, 1984 <br />SUBJECT:Review of Septic Testing Report Submitted for #816, Lake <br />Minnetonka Homes Subdivision <br />I have reviewed the information submitted and wish to make the following <br />comments: <br />Lot 1, Blr^k 1 - testing for this lot was reviewed by me on August 26, <br />1983, with the following comments: <br />The tested sites are located centrally within this lot. Both primary and <br />alternate sites are suitable for a shallow trench drainfield system (no <br />deeper than ].8"). Due to somewhat high water tables (mottling observed <br />at 2’9" in one hole, 3*5* to 5*5* in others) a curtain drain will be necessary <br />on this site at a depth at least 3' below the trenches. No other sites <br />on the lot appear suitable for a trench drainfield system, so these sites <br />must be preserved. Extra care must be taken in house placement since <br />the sites are centrally located on the lot. A system design for a five- <br />bedroom home has been submitted. <br />Lot 1, Block 2 - testing for this lot was reviewed by me on August 26, 1983, <br />with the following comments: <br />The tested sites are in the northwest corner of the lot. Primary and <br />alternate sites are adjacent to each other. Mottling was noted at depths <br />ranging from 42" to 56" indicating some seasonal saturation. The sandy <br />soil types indicated and the genreal slope to the south will allow the use <br />of a shallow trench drainfield on both primary and alternate sites as long <br />as a curtain drain is installed. The average perc rate for the entire <br />site is about 10 MPI. A pumping station will be needed to deliver effluent <br />to the tested drainfield sites. A suitable design proposal for a five- <br />bedroom home has been submitted. <br />Lot 2, Block 2 - the testtid sites are located in the southeast corner of <br />the lot. Primary and alternate sites both were found to contain sandy to <br />silty loam soils, with perched water tables which can be eliminated by use <br />of curtain drains. Perc rates averaged 7.5 MPI. The sites will both <br />likely be suitable for gravity flow from the houses. Care must be taken <br />to preserve the sites due to their location near the proposed road. A <br />system design for a five-bedroom home has been submitted. <br />Lot 1, Block 3 - the tested sites are located on the east central portion <br />of the lot. Soils indicated were loams and sandy loams. Again, layering <br />of the soils has created perch seasonal water tables which can be eliminated <br />Septic T <br />April 12 <br />Page 2 <br />by use c <br />these dr <br />submitte <br />Lot 2, I <br />the lot <br />central] <br />use of c <br />these It <br />trenches <br />are not <br />and hen( <br />In summi <br />alterna <br />on thes< <br />the pro; <br />on the <br />recomme <br />and rop <br />constru
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